Efficient and cost-effective drilling of directional wells necessitates the implementation of best drilling practices and advanced techniques to optimize drilling operations. Failure to adequately consider drilling risks can result in inefficient drilling operations and non-productive time (NPT). Although advanced drilling techniques may be expensive, they offer promising technical solutions for mitigating drilling risks. This paper aims to demonstrate the effectiveness of advanced drilling techniques in mitigating risks and improving drilling operations when compared to conventional drilling techniques. Specifically, the advanced drilling techniques employed in Buzurgan Oil Field, including vertical drilling with mud motor, managed pressure drilling (MPD), rotary steerable system (RSS), and expandable liner hanger (ELH), are investigated and evaluated through case study analyses, comparing their performance to that of conventional drilling techniques. The findings indicate that vertical drilling with mud motor exhibits superior drilling performance and wellbore verticality compared to conventional rotary drilling bottom hole assemblies (BHA) for drilling the 17 ½" hole section. MPD systems employed in the 12 ¼" hole section demonstrate safe drilling operations and higher rates of penetration (ROP) than conventional drilling methods. Rotary steerable systems exhibit reduced tortuosity and achieve higher ROP when compared to mud motor usage in the 8.5" and 6" hole sections. Lastly, investigations of expandable liner hanger cases reveal subpar cement quality in the first case and liner remedial work in the second case, highlighting the successful implementation of ELH techniques in the offset field. Overall, this paper highlights the advantages of utilizing advanced drilling techniques in Buzurgan Oil Field, showcasing their ability to mitigate drilling risks and enhance drilling operations when compared to conventional drilling approaches.
Zubair oilfield is an efficient contributor to the total Iraqi produced hydrocarbon. Drilling vertical wells as well as deviated and horizontal wells have been experiencing intractable challenges. Investigation of well data showed that the wellbore instability issues were the major challenges to drill in Zubair oilfield. These experienced borehole instability problems are attributed to the increase in the nonproductive time (NPT). This study can assist in managing an investment-drilling plan with less nonproductive time and more efficient well designing.
To achieve the study objectives, a one dimension geomechanical model (1D MEM) was constructed based on open hole log measurements, including Gamma-
... Show MoreDifferent additives are used in drilling fluids when the demanded properties cannot be gotten with clays. Drilling muds needs several additives and materials to give good characteristics. There are local alternatives more suitable for enhancing the rheology and filtration of drilling fluids. An experimental work had been conducted to assess the suitability of using potato starch to enhance rheological properties and filtration in drilling mud. This study investigated the potato starch as a viscosifier and fluid losses agent in drilling fluid. Results from this study proved that rheological properties of potato starch mud increased when pH of drilling fluid is increased. Potato starch could be used to enhance gel strength at low pH
... Show MoreDifferent additives are used in drilling fluids when the demanded properties cannot be gotten with clays. Drilling muds needs several additives and materials to give good characteristics. There are local alternatives more suitable for enhancing the rheology and filtration of drilling fluids. An experimental work had been conducted to assess the suitability of using potato starch to enhance rheological properties and filtration in drilling mud. This study investigated the potato starch as a viscosifier and fluid losses agent in drilling fluid. Results from this study proved that rheological properties of potato starch mud increased when pH of drilling fluid is increased. Potato starch could be used to enhance gel strength at low pH
... Show MoreGas-lift technique plays an important role in sustaining oil production, especially from a mature field when the reservoirs’ natural energy becomes insufficient. However, optimally allocation of the gas injection rate in a large field through its gas-lift network system towards maximization of oil production rate is a challenging task. The conventional gas-lift optimization problems may become inefficient and incapable of modelling the gas-lift optimization in a large network system with problems associated with multi-objective, multi-constrained, and limited gas injection rate. The key objective of this study is to assess the feasibility of utilizing the Genetic Algorithm (GA) technique to optimize t
Several directional wells have been drilled in Majnoon oilfield at wide variation in drilling time due to different drilling parameters applied for each well. This technical paper shows the importance of proper selection of the bit, Mud type, applied weight on Bit (WOB), Revolution per minute (RPM), and flow rate based on the previous wells drilled. Utilizing the data during drilling each section for directional wells that's significantly could improve drilling efficiency presented at a high rate of penetration (ROP). Based on the extensive study of three directional wells of 35 degree inclination (MJ-51, MJ-52, and MJ-54) found that the applied drilling parameters for MJ-54 and the bit type within associated drilling parameters to drill
... Show MoreIn present work an investigation for precise hole drilling via continuous wave (CW) CO2 laser at 150 W maximum output power and wavelength 10.6 μm was achieved with the assistance of computerized numerical controlled (CNC) machine and assist gases. The drilling process was done for thin sheets (0.1 – 0.3 mm) of two types of metals; stainless steel (sst) 321H, steel 33 (st). Changing light and process parameters such as laser power, exposure time and gas pressure was important for getting the optimum results. The obtained results were supported with computational results using the COMSOL 3.5a software code.
In this research, a qualitative seismic processing and interpretation is made up
through using 3D-seismic reflection data of East-Baghdad oil field in the central part
of Iraq. We used the new technique, this technique is used for the direct hydrocarbons
indicators (DHI) called Amplitude Versus Offset or Angle (AVO or AVA) technique.
For this purposes a cube of 3D seismic data (Pre-stack) was chosen in addition to the
available data of wells Z-2 and Z-24. These data were processed and interpreted by
utilizing the programs of the HRS-9* software where we have studied and analyzed
the AVO within Zubair Formation. Many AVO processing operations were carried
out which include AVO processing (Pre-conditioning for gathe
In the present work advanced oxidation process, photo-Fenton (UV/H2O2/Fe+2) system, for the treatment of wastewater contaminated with oil was investigated. The reaction was influenced by the input concentration of hydrogen peroxide H2O2, the initial amount of the iron catalyst Fe+2, pH, temperature and the concentration of oil in the wastewater. The removal efficiency for the system UV/ H2O2/Fe+2 at the optimal conditions and dosage (H2O2 = 400mg/L, Fe+2 = 40mg/L, pH=3, temperature =30o C) for 1000mg/L load was found to be 72%.
Background: Plantar heel pain is a clinical syndrome characterized by pain and tenderness beneath the heel which is typically worse in the morning and improves after the first few steps in the day. It is a common and frequently disabling clinical complaint that may be caused by a broad spectrum of osseous or soft tissue disorders. Objective: To evaluate the effectiveness of an operation of multiple drilling of calcaneum for resistant plantar heel pain syndrome. Methods: During the period from November 2012 to August 2016, 17 patients (17heels) were enrolled in a cohort clinical study at the orthopedic unit in AL-Sheikh Zayed and AlWassity Hospitals. Result: Drilling of the calcaneum is a simple procedure achieving 70.6% cure in resistant as
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